In Re. Investigation of an Accident
which Occurred on the Oregon-Washington Railroad & Navigation
Company’s line, near Biggs, Ore., Mar. 10, 1916.
.
On March 10, 1916, there was a derailment of a freight train
on the Oregon-Washington Railroad & Navigation Company’s
line near Biggs, Ore., which resulted in the death of 2 employees
and the injury of 1 employee. The investigation of this accident
was made in conjunction with the Railroad Commission of the
State of Oregon, and as a result of this investigation the
Chief of the Division of Safety submits the following report.
The accident occurred on the Shaniko Branch, extending from
Biggs to Shaniko, at a point about 3 miles east of Biggs.
This is a single track line and trains are operated by time-card
and train orders. From Klondike to Gibson, a distance of 8.9
miles, the grade is descending for west-bound trains practically
the entire distance, most of it being from 1% to 2%, while
at two places it is about 2.25% for a distance of 2,000 feet
at each point. From Gibson to Biggs, 4.9 miles, the greater
part of the grade is in excess of 3%, ranging from 3% to 3.47%.
At the point of accident the track is on a 14-degree curve
extending to the left for west-bound trains, the maximum super
elevation being 3 degrees. The track is laid with 60 and 75-1b.
rail, with from 18 to 20 ties under each rail. Tie-plates
and rail-braces are used, and the track is in good condition
for branch line service. The maximum speed allowed for freight
trains between Klondike and Gibson is 12 miles an hour, and
10 miles an hour between Gibson and Biggs. The weather at
the time was clear.
Westbound freight train extra 142 consisted of 8 loaded cars
and a caboose, hauled by locomotive 142, and was in charge
of Conductor Dalrymple and Engineman Williamson, and was derailed
at about 2:25 a.m. while rounding the 14-degree curve. At
this point the 5 cars behind the first car were derailed,
thrown down the embankment and demolished. The 2 rear cars
and the caboose remained on the roadway, with all the wheels
off the rails except the rear trucks of the caboose. The locomotive
and the first car of the train traveled an additional distance
of about 3,700 feet before being derailed on a curve to the
right of 10 degrees, both the locomotive and the car being
quite badly damaged.
Engineman Williamson stated that in stopping at Gibson he
made a full service application of the air-brakes and left
the brakes set while the train was being inspected. The stop
at this point was made without the use of handbrakes, the
retainers having been turned up leaving Klondike. After he
had oiled the locomotive the fireman told him they were ready
to go. Engineman Williamson whistled off, released the brakes,
and then waited until the full pressure had been pumped up,
the train-line pressure at the time of departure being nearly
75 pounds, while the main reservoir pressure was 85 pounds.
He then worked sufficient steam to get the train started,
leaving Gibson without any of the brakemen having told him
whether or not all of the air-brakes were working. As soon
as the speed increased he made an application of the air-brakes.
This first application was made at a point about 1/4 of a
mile from Gibson, and was a 15-pound application, and when
at a point nearly 1 mile from Gibson was followed by an additional
application of 10 pounds, the brakes not being released after
the first application. At the time the first application was
made the speed was about 7 miles an hour, and it was about
5 or 6 miles an hour when the second application was made,
at which time the two brakemen and the conductor were on top
of the train setting handbrakes with their clubs. Engineman
Williamson said that he could not see the man on the rear
of the train, but was watching the head brakeman setting the
brakes on the first car, and when he had apparently finished
and was starting back toward the second car he released the
air-brakes, at which time the speed was about 6 miles an hour.
After releasing the brakes he placed the brake valve in the
full release position and then noticed that the train-line
pressure was close to 70 pounds. He then saw the hands on
the air-pressure indicator going down, but at first he did
not pay much attention to this, saying that usually when the
air started to go back in the train the hands on the indicator
would drop a little. When the indicator showed that the pressure
had dropped about 10 pounds he thought the train-line had
broken, and then placed the brake valve in the lap position,
at which time the train-line pressure was about 60 pounds.
Just as he did so he saw that it was the main reservoir pressure
which had gone down, and he said that he could hear the air
blowing immediately under the cab of the locomotive. The reservoir
pressure had decreased about 40 pounds and the speed of the
train was increasing, so he placed the brake-valve in the
emergency position, and as he did so sounded one long blast
of the whistle and told the fireman to jump off, that he thought
the train was running away, and that he had no air. The fireman
said that they were not going very fast, and that probably
the engineman could stop the train. Engineman Williamson stated
that he then tried twice to reverse the locomotive, but that
the reverse lever did not hold, the quadrant being a little
worn. At this time the speed was such that he could not pull
it back again, and he again told the fireman to jump. Engineman
Williamson also stated that on account of having just released
the brakes there had not been time to recharge them, and if
the brakes had been recharged he felt sure that with the amount
of train-line pressure carried he would have been able to
stop the train. Engineman Williamson said that in his opinion
the accident was caused by the breaking of the main reservoir
air-pipe. With regard to the reverse lever slipping out of
the notch in the quadrant, he stated that he had never had
this trouble before, but that on this trip it had worked out
of the notch two or three times when the locomotive was working
heavily. He further stated that he had been running on this
branch about two months; he had never had any other experience
on a mountain railroad.
Head Brakeman Strong stated that the train was doubled up
the hill into Sendon, the first station east of Klondike.
When the train was coupled together he coupled the air-nose
himself and cut in the air, but no test of the air-brakes
was made at this point. He also turned up the retainer valves
on all of the cars when leaving Klondike for Gibson. he stated
that it was the custom to stop at Gibson by use of the air-brakes
and to walk along the train to see if the pistons were out
not less than 8 inches nor more than 8 inches. One man would
start from one end of the train and another man from the other
end, and after they met a proceed signal would be given from
the rear end. When the stop was made at Gibson no separate
test of the air-brakes was conducted, the engineman stopping
the train and leaving the brakes applied. Brakeman Strong
stated that he then walked back on the engineman's side of
the train and examined 4 or 5 cars, finding the pistons to
be out on all of them. When about the middle of the train
he met either Brakeman Stimpson or Conductor Dalrymple, who
was on the opposite side of the train and had been examining
the cars, working forward from the rear of the train. A proceed
signal was then given from the opposite side of the train,
either by Conductor Dalrymple, or by Brakeman Stimpson, who
was killed in the accident. Brakeman Strong also stated that
he did not look over the train after the brakes were released
to observe the piston travel, and he did not know how long
the train had stopped at Gibson, but thought it was 3 or 4
minutes. As soon as the train left Gibson they began applying
hand-brakes. He also felt the air-brakes being applied, but
did not notice how fast the train was traveling at that time.
This application reduced the speed to about 6 or 8 miles an
hour, and he said that the train then seemed to get a start
and to travel faster and faster, until it was running away.
When the train had proceeded about three-quarters of a mile
the engineman whistled for brakes. At this time all of the
hand-brakes were set. Two of them did not work well, but he
did not remember on which cars they were located. At first
he did not think the train was running away, but when he noticed
the speed he thought that it was about 15 miles an hour, and
possibly more. Head brakeman Strong stated that he had been
in the employ of the company since February 11, 1916, practically
all of which time he had spent on the Shaniko Branch. He had
been a brakeman on other roads since 1912, and had had a few
months' experience on mountain grades on the Chicago. Milwaukee
& St. Paul and Northern Pacific Railways.
Conductor Dalrymple stated that the retainers were usually
turned up when coming into Klondike. with the exception of
the retainer on the caboose, which was turned up at Gibson,
and while he personally did not know when they had been turned
up on this session he had complete confidence in the brakemen,
and thought the retainers were turned up, saying that he could
smell the heat from the wheels and could also tell by the
way the train was traveling. When at Gibson, the train was
inspected for the purpose of observing the piston travel,
and he assisted in this, working forward from the rear of
the train; at the time of this inspection the retainers were
turned up. He stated that if the piston travel was over 7
or 8 inches the slack would be taken up. After the inspection
had been completed a proceed signal was given by Brakeman
Simpson. Conductor Dairymple said that the usual air test
at Gibson is for the engineman to keep the brakes applied
until the train is inspected, then to wait until the air is
pumped up before proceeding. In this particular case he thought
the train was at Gibson about 5 minutes before it proceeded,
and when his attention was called to the fact that his delay
report showed his train to have been at Gibson 15 minutes
he said that this was put down after the accident and that
he was just guessing at the time. Conductor Dalrymple said
that after leaving Gibson he set two hand-brakes on the rear
of the train, set the caboose brake, and turned up the retainer
on the caboose. While in the caboose he noticed that the air-pressure
was 80 pounds. he then went out on top of the train, and while
there felt what he thought was an ordinary application of
the air-brakes, and he stated that it reduced the speed from
about 10 miles an hour, when the application was made, to
about 5 or 6 miles an hour. He did not feel any application
of the brakes other than this one application, saying that
after the brakes were released the speed of the train kept
increasing and he was wondering why the brakes were not again
applied. Conductor Dairymple also said that before the brakes
were released he and the two brakeman were on top of the cars
and had set the band-brakes, and that before the engineman
whistled for brakes the two brakemen had doubled on the hand-brakes
on the head end of the train, and the head brakeman then came
back and doubled with him on the hand-brakes on the rear cars.
He did not notice what the speed was when the engineman called
for brakes, as he was busy setting the hand-brakes. He also
said that he noticed nothing wrong with the hand-brakes. Conductor
Dalrymple had been running this train for about a week. He
stated that in 1910 he had been a brakeman on this branch
for a period of about 9 months, and since that time had often
been over it as an extra conductor. He also said that Brakeman
Stimpson had been on this run 23 days, that he was a good
brakeman and understood his business.
Assistant Superintendent Coykendall stated that the practice
was to set all hand-brakes as soon as the train started from
Gibson, and as soon as an application of the air-brakes was
made the train crew would tighten the hand-brakes, taking
up the slack caused by the application of the air-brakes.
If this was done properly the hand-brakes would be applied
as tightly as if by a service application, and a train could
go down the hill without a further application of the air-brakes
being made. In this case he did not think the hand-brakes
were set when starting down the hill.
Traveling Engineer Rifer stated that he took off the caps
of three of the triple valves and tested two other cars, and
he found the braking equipment on the train was first-class
in every particular. All of the brake-shoes on the engine
and tender were blue and burned, indicating that the brakes
had been in working order at the time of the accident. The
retainer on the first car behind the locomotive was half way
up and the triple valve in full service application, but the
brake-shoes and wheels did not show any signs of high braking
power. On the second car the triple valve was in service lap
position, while the retainer could not be found; the third
car had the retainer half way up, with the brake chain wound
around the brake shaft; the fourth car had the retainer up
and the triple in service position; the fifth car had the
retainer turned up, while the triple valve could not be reached;
on the sixth car the retainer and triple could not be located,
while on the seventh car the retainer was half way up and
the brake-chain wound around the brake shaft. On each of these
last six cars the wheels were blue and the brake-shoes red,
indicating that the brakes had been in working condition.
A test of the 5th car showed that the piston travel was 6
inches, and the retainer held for 1 minutes 30 seconds after
the release of the brakes. On the caboose the piston travel
was 6 inches, and the retainer held 1 minute 15 second after
release. Mr. Rifer also stated that he found several broken
pipes on the engine, but these apparently were broken in the
accident. The breaks were new and had the appearance of having
been broken off instead of pulled out, with the exception
of the main reservoir pipe on the rest of the tender, which
had the appearance of having been pulled out. This pipe was
pulled out at the threads, however, and could have been pulled
out when the tender became separated from the tender frame.
If this particular pipe had broken while coming down the mountain,
at a time when the brake-valve was in release position, the
brakes would have been applied automatically. He also said
that he found the pipe broken from the auxiliary reservoir
on the engine underneath the cab floor on the engineman's
side, and he said that if this had broken while the train
was coming down the mountain, with the brake-valve in the
release position, it would help drain the main reservoir and
overcome the leak, helping to apply the air-brakes. There
was nothing which he could find to explain the statement of
the engineman about the air leaking away after the brakes
were released, and he said that any air pipe which broke and
allowed the air to escape would cause the brakes to apply.
He did not think the engineman lost control of the train on
account of defective equipment, but that the train was traveling
too fast when it struck the heavy part of the grade, before
they began to apply the hand-brakes, and that when the brakes
were all applied and the engineman began to release the air,
the speed of the train increased and could not be controlled.
The inspection record of locomotive 142, made on March 8,
showed the brakes to be it good condition, while the main
reservoir pressure was 90 pounds and the brake pipe pressure
70 pounds. Mr. Rifer stated that he had ridden with Engineman
Williamson on the Shaniko branch two or three days prior to
the accident, and he considered him to be a competent man
for service on this branch.
Roundhouse Foreman Quins stated that on February 16, 1916,
a practically new air pump was applied to locomotive 142,
this pump being tested on the day it was applied. The gauge
and brake valve were tested on January 5th, and the triple
on January 6th, while the brake cylinder was cleaned on January
6th. In examination of the locomotive after the accident he
found the cut-out valve in the train-line, under the engineman's
valve, shut tightly, and he thought it was closed by the engineman
striking it with his foot when trying so reverse the locomotive.
Car Foreman Hails said that in looking over the wreckage he
found the brake-rod on the first car tied up with wire. This
would permit the easier piston travel, and would result in
the brake on this car not amounting to much and would also
affect the hand-brake on one end of the car. He stated that
the wheels of all the cars, except the first, were blue.
Mr. A. W. Perlay, a special representative of the mechanical
department, said that according to the engineman's statement
there was 70 pounds train-line pressure when the engineman
heard the explosion under the cab, at which time the brake
valve was in the full release position. He thought that the
reservoirs surely must have been charged to 60 or 65 pounds,
and would take only 7 or 8 seconds to recharge the train of
8 cars. He, therefore, was of the opinion that if any of the
pipes on the engine had broken the air-brakes would have been
applied automatically.
Mr. J. T. Lengley, assistant superintendent of motive power,
stated that he found the retainer down on the car next to
the caboose, and he thought there was one other car in the
wreckage on which the retainer was down. With reference to
the cause of the accident, it was his opinion that, after
the engineman released the brakes, the train was allowed to
attain a rate of speed higher than it should have traveled,
and that with the train-line pressure carried the engineman
should have been able to stop the train, regardless of the
broken air pipe, had not the speed been excessive.
On account of the badly damaged condition of the locomotive
hauling this train, and the further fact that all of the cars
except two were practically destroyed, no proper test could
be made to determine the efficiency of the air-brake equipment.
The evidence indicates, however, that the air-brakes on the
first car were of doubtful efficiency, and that, with one
exception, all of the hand-brakes were working, while the
employees state that they were applied, brake clubs being
used for the purpose, and the burned condition of the car
wheels and the brake-shoes is evidence that the brakes had
been applied. If the hand-brakes on this train had been properly
applied, however, as soon as it left Gibson, and if the engineman's
statement is correct that after placing the brake valve in
full release position the train line was recharged to nearly
70 pounds, then the speed limit of 10 miles an hour should
have been observed and the train operated down the mountain
in safety.
It is believed that this accident was caused by the crew in
charge of this train permitting it to attain a speed in excess
of the 10 miles an hour prescribed by rule and that it got
such a start that they were unable to control it by using
both the hand-brakes and air-brakes.
Engineman Williamson had been employed by the Southern Pacific
company as a fireman for about four years, resigning in August,
1905. In October, 1905, he entered the service of the Oregon-Washington
Railroad & Navigation Company as a fireman, being discharged
in September, 1906, for neglect of duty. He was reinstated
November 28, 1906, and in 1912 was promoted to engineman.
His record was good. Conductor Dalrymple was employed for
three years by the Northern Pacific Terminal Company as a
wiper. In 1907 he entered the service of the Oregon-Washington
Railroad & Navigation Company as a wiper being promoted
the same year to switch engine fireman, and then to road fireman.
In 1908 he resigned, and in 1910 was reemployed as a brakeman,
being promoted to conductor in 1914. His record was good.
Head Brakeman Strong was employed on February 11, 1916, and
had a clear record. In the proceeding 5 1/2 years he had been
employed eight different times by six different railroads.
Rear brakeman Stimpson was employed as a brakeman on December
3, 1913, and had a clear record. He had had about four year's
experience with other roads.
At the time of the accident these employees had been on duty
about 15 1/2 hours, after over 14 hours off duty.
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