IN RE INVESTIGATION OF AN ACCIDENT
WHICH OCCURRED ON THE LOS ANGELES AND SALT LAKE RAILROAD,
UNION PACIFIC SYSTEM, NEAR SANDY, UTAH, ON JULY 15, 1923.
On July 15, 1923, there was a derailment of a passenger train
on the Los Angeles and Salt Lake Railroad, Union Pacific System,
near Sandy, Utah, which resulted in the death of 3 employees,
and the injury of 10 passengers, 1 employee, and 2 trespassers.
This accident was investigated in conjunction with representatives
of the Public Utilities Commission of Utah.
Location and method of operation.
This accident occurred on the Provo sub-division of the Salt
Lake Division, a single-track line extending between Salt
Lake City and Lynndyl, Utah, a distance of 134.1 miles, over
which trains are operated by time-table and train orders,
no block-signal system being in use. The point of accident
was about 1 1/2 miles west of Sandy; approaching this point
from the east the track is tangent for a distance of 2,502
feet, followed by a curve of 1 degree to the left which is
505 feet in length, the accident occurring on this curve near
its leaving end. The grade is 0.75 per cent descending for
a distance of 1,500 feet and then there is a vertical curve
600 feet in length leading to an ascending grade, the point
of accident being near the beginning of the ascending grade.
The track is laid with 90-pound rails, 33 feet in length,
with an average of 18 treated ties to the rail-length, tie-plated,
single-spiked, and ballasted with 3 or 4 inches of gravel;
it is maintained in good condition. The weather was clear
at the time of the accident. which occurred at 12.42 a.m.
Description.
Westbound passenger train No. 3 consisted of five baggage
cars, one coach, one chair car, one tourist sleeping car,
one Pullman sleeping car, and one business car, hauled by
engine 3174, and was in charge of Conductor Valiant and Engineman
Runswick. The second, fifth, and sixth cars were of wooden
construction, while the others had steel underframes. Train
No. 3 left Sandy at 12.32 a.m., two minutes late, and was
derailed west of Sandy while traveling at a speed estimated
to have been 25 or 30 miles an hour.
The engine came to rest on the left side of the track, bottom
up, at the foot of a 35-foot embankment, with the tender partly
under the engine. The first five cars were derailed at the
time of the accident. while the sixth car tipped over about
35 minutes afterwards; the second car was derailed to the
right, while the others were derailed to the left. The second
and third cars were practically demolished. The employees
killed were the engineman, fireman, and a student fireman.
Summary of evidence.
Conductor Valiant and Brakemen Marcott and Wing said they
noticed no application of the air brakes prior to the derailment
of the train, which was moving at a speed estimated by them
to have been from 25 to 30 miles an hour. On examining the
track they found water running in the drainage ditch on the
left side of the track, and also found that the track had
been undermined by the water. They estimated the stream of
water in the ditch to have been 5 or 6 feet in width and varying
in depth from a few inches to a foot.
On the south side of the track. referring to time-table direction,
and about 180 feet distant from it, is a farm irrigated by
water obtained from an irrigation ditch which is on the south
side of the farm. To irrigate a tract of the size of this
farm, the water is used for a period of nine hours, usually
once every seven or eight days. The stream of water thus used
is about 2 feet wide and 18 inches in depth. The water not
absorbed by the soil runs off at the north end of the farm
and flows northward to the railroad track, at which point
there is a 10-inch iron pipe to carry the water under the
track and thence to a canal about 150 feet distant. On the
south side of the track there is a ditch running parallel
to the track to carry off drainage water from the right of
way. This ditch extends westward for a distance of approximately
900 feet to where it reaches the 35-foot fill where the accident
occurred.
On the night of the accident water to irrigate the farm had
been turned on at about 10.20 p.m., no further attention being
paid to it until after the accident occurred, when the owner
of the farm was notified of the accident and then turned off
the water. Examination showed that the iron pipe under the
track had become clogged and that the water, instead of being
carried under the track to the canal, had become diverted
to the drainage ditch on the south side of the track and had
flowed through that ditch for a distance of several hundred
feet before it finally washed away the fine sandy soil on
which the track is laid, undermining the left side of the
track for a considerable distance. It further appeared that
a dike had been erected by the owner of the farm on the side
of his land nearest the railroad track in order to back up
the water and irrigate one portion of the land which was higher
than the rest of it; this dike, however, had broken and the
soaked condition of the soil indicated that in some places
the stream of water thus released and flowing toward the railroad
track had been about 30 feet in width. In addition it also
appeared that the land undoubtedly had not absorbed as much
of the water as usual. as it had been irrigated only three
days previously by someone having turned on the water in the
absence of the owner. It also appeared that on the night of
the accident, although the full flow of water was being used,
yet only one-half of the land was being irrigated.
The owner of the farm said that on a previous occasion he
had noticed that the pipe under the track had become clogged
so that water could not pass through it, and at that time
he had turned off the water but did not notify the railroad
authorities concerning the condition of the pipe. Section
Foreman Dow also said that on two occasions he had been notified
by the dispatcher that there was water running over the track
at this point, once about a year previously and the other
time about a month previously, and while on reaching the spot
he found that the water had gone down, due to the obstruction
in the pipe evidently having cleared itself, yet the ballast
was wet and showed that the water had been on the track, he
said he had reported it to the roadmaster, but the latter
said he did not recall any trouble of this kind at this point,
which statement was also made by Division Engineer Strong.
Conclusions:
This accident was caused by a washout.
The water causing this washout came from an irrigation ditch,
the full flow of which was being used although only half of
the farm was being irrigated, and this flow of water, coupled
with the breaking of the dike and possibly causing it to break,
undoubtedly resulted in an unusual amount of water being carried
toward the railroad track, and when the pipe intended to carry
it under the track became clogged, this water found its way
to the drainage ditch parallel to the track and ordinarily
used only for draining the right of way. This water then flowed
through that ditch for several hundred feet to where it washed
away the side of the embankment, undermining the track and
causing it to give way under the head end of the train.
The fact that this ditch had become clogged on previous occasions
indicates that it was not large enough to allow a sufficient
margin of safety in case there should be an unusual amount
of water flowing toward the track, and immediate steps to
remedy such a condition should be taken.
At the time of the accident none of the employees involved
had been on duty in violation of any of the provisions of
the hours of service laws.
|